Northwire Canada EditionSunday, July 12, 2026
Northwire
GLDN 0.055 +0.0% BRON 0.040 +0.0% BTO 5.43 −0.7% ESK 0.365 −2.7% AUMN 0.275 +0.0% GGX 0.040 +0.0% S 0.155 +29.2% NNX 0.035 +0.0% ABX 51.90 −0.6% TTS 2.40 −4.0% FCI 0.400 −9.1% GR 0.075 +0.0% AII 23.38 +12.4% TUNG 1.72 +1.8% LGO 1.01 −2.9% EMM 0.080 +0.0% GLDN 0.055 +0.0% BRON 0.040 +0.0% BTO 5.43 −0.7% ESK 0.365 −2.7% AUMN 0.275 +0.0% GGX 0.040 +0.0% S 0.155 +29.2% NNX 0.035 +0.0% ABX 51.90 −0.6% TTS 2.40 −4.0% FCI 0.400 −9.1% GR 0.075 +0.0% AII 23.38 +12.4% TUNG 1.72 +1.8% LGO 1.01 −2.9% EMM 0.080 +0.0%
Production / Operations

TIDEWATER RENEWABLES LTD. COMPLETES PLANNED OUTAGE AT ITS RENEWABLE DIESEL REFINERY AND RETURNS TO FULL CAPACITY

LCFS · Price

Executive Summary

  • Tidewater Renewables completed a seven‑day planned outage at its renewable diesel and hydrogen complex in Prince George, BC, reinstalling a rebuilt component.
  • Utilization has returned to full capacity of 3,000 barrels per day after the outage, up from an interim average of ~2,250 bbl/d during temporary repairs.
  • The outage follows a short unplanned shutdown (Oct 15‑29, 2025) caused by an equipment anomaly that was temporarily repaired pending component rebuild.

Key Details

  • Planned Outage Duration: 7 days (Dec 6 – Dec 12, 2025).
  • Complex Affected: Renewable Diesel & Renewable Hydrogen Complex (“HDRD Complex”) in Prince George, BC.
  • Component Work: Faulty component removed, rebuilt off‑site, and safely reinstalled during the outage.
  • Utilization Pre‑Outage: Approx. 2,250 barrels per day (Nov 1 – Dec 5, 2025) with temporary repair in place.
  • Post‑Outage Utilization: Returned to full design capacity of 3,000 barrels per day as of Dec 12, 2025.
  • Previous Unplanned Outage: Oct 15 – Oct 29, 2025 due to equipment anomaly; temporary repair allowed limited production.

Notable Quotes

(No direct quotes were provided in the release.)

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